Sewer pipe cylinder liner
I
couldn't afford to have the cylinder resleeved so I put the engine in
my 'toohard' basket and moved on to cleaning up my scrap heap. During
this clean-up I was about to throw away an old cast iron sewer pipe
when I looked more carefully at the size of it and put it down. I got
my calipers and found it measured about half an inch oversized and
inside .040 under for the International Famous cylinder.
I then
went to see Bert Knight, a retired engineer who used to run the local
power station, operating such engines as an eight-cylinder Harland &
Wolfe and Ruston Hornsbys.
I
explained my problem to Bert and asked if it would be possible to
make a cylinder liner from a sewer pipe. He thought we could try and
was willing to help. This was good news because Bert owns a larger
lathe than mine and this was needed. After inspecting the crankshaft
Bert agreed that the way out was to machine down the main bearing
jounals and sleeve it back to standard.
We
decided to repair the crankshaft first. The shaft was machined, then
the steel sleeve was made and shrunk on to the shaft. Bert machined
it to .005 oversized to make up for the wear in the bronze bearings.
Next
on to the cylinder lining. First I made a centre for the sewer pipe
on my small lathe, then we set up Bert's lathe and, after many hours,
we had a liner machined on the outside.
We
planned to bore out the cylinder to take the liner on the lathe but
the cylinder was too large, so it was off to Staube Engineering in
Mildura who did an excellent job for me at a reasonable price.
I
then found the liner a bit tight, so I honed the cylinder until the
liner would almost go in by hand, gave it a coat of high temperature
Loctite and pressed it in.
Honing for the perfect piston fit
Because
there was only .040 on the inside to play with I machined the piston
to .010 under and my son Shane and I honed the cylinder to fit the
piston, using a deglazing hone. It took six-and-a-half hours, taking
turns on the drill and when the drill ran hot we changed drills. It
was sure hard to remove .030 this but way the result was a perfect
fit.
DIY rings recipe
It
was then time to make the rings. I used a cylinder liner from a
Cummins truck. I don't know if this is the correct procedure for
making rings but it works OK, as follows:
First
machine a ring .030 oversize, cut with a hacksaw and wedge open with
a steel wedge bolt between two ½ in plates and heat in a forge to a
dull red and let it cool. Make a false cylinder .030 oversize and fit
the ring and clamp in a closed position. Remove it from the false
cylinder and machine to the size of the cylinder. It should then be a
good sealing ring.
Getting it together
While
all this was taking place I was given an igniter and then a Webster
low tension magneto. Next came the paint job and construction of the
petrol tank and cooling tower.
The
engine was then assembled and started, approximately three months
after the recovery trip.
The
nameplate reads: "International Harvester eng. No B2654 8 h.p.
R.P.M. 275"
I
have now run it for many days and the cylinder and rings are
working well.
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